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Lead Application to Cure Sap Wells by Deploying Straddle Packer, Success Story

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Abstract Objective/Scope The Increase of inactive wells due to subsurface integrity issue is observed in brown fields, Fig-1 is, showing the record for onshore UAE asset, the economic challenges is calling for alternative solutions to restore well integrity with lower cost. Straddle packer application is consists of two tandom packers with spacer pipe in between with anchoring system deployed riglessly in the well to isolate the communication point between Ann A and Tubing.Fig-2, Methods, Procedures, Process Communication between tubing and annulus A (Failure of primary barrier) is identified as the right candidate wells for straddle packer application, First step is to clearly identify the point of communication, it has been done by annulus pressure investigation excersize during flowing and shut in condition, observing the return of annulus fluid which was the same produced gas Noise log has been conducted and clearly identified the communication point at SPM (Side Pocket Mandrel) to be used for emergency killing, Tubing integrity test was conducted using nippless plugs and inflow test below and above the leak point and confirm no other leak points within the tubing Engineering drawing for the leaking assembly was reviewed to design the dimension of straddle packer assembly, length and packer size It is recommended to deploy the assembly using electric line correlation for accurate depth selection After setting annulus pressure observed no build up Well opened safely to production Results/Observation/Conclusion Leak point arrested, well primary barrier restored Removed from DWS (drilling and workover schedule) and restore well production in addition to improving inactive string KPI for Gas asset Save almost work over cost for gas well XX-197 Novel/ Additive information The way forward is to check the scalability of extending this application among other ADNOC assets and to screen the right candidate wells for this application To add this application as a part of well integrity procedures and recommendations for such like cases
Title: Lead Application to Cure Sap Wells by Deploying Straddle Packer, Success Story
Description:
Abstract Objective/Scope The Increase of inactive wells due to subsurface integrity issue is observed in brown fields, Fig-1 is, showing the record for onshore UAE asset, the economic challenges is calling for alternative solutions to restore well integrity with lower cost.
Straddle packer application is consists of two tandom packers with spacer pipe in between with anchoring system deployed riglessly in the well to isolate the communication point between Ann A and Tubing.
Fig-2, Methods, Procedures, Process Communication between tubing and annulus A (Failure of primary barrier) is identified as the right candidate wells for straddle packer application, First step is to clearly identify the point of communication, it has been done by annulus pressure investigation excersize during flowing and shut in condition, observing the return of annulus fluid which was the same produced gas Noise log has been conducted and clearly identified the communication point at SPM (Side Pocket Mandrel) to be used for emergency killing, Tubing integrity test was conducted using nippless plugs and inflow test below and above the leak point and confirm no other leak points within the tubing Engineering drawing for the leaking assembly was reviewed to design the dimension of straddle packer assembly, length and packer size It is recommended to deploy the assembly using electric line correlation for accurate depth selection After setting annulus pressure observed no build up Well opened safely to production Results/Observation/Conclusion Leak point arrested, well primary barrier restored Removed from DWS (drilling and workover schedule) and restore well production in addition to improving inactive string KPI for Gas asset Save almost work over cost for gas well XX-197 Novel/ Additive information The way forward is to check the scalability of extending this application among other ADNOC assets and to screen the right candidate wells for this application To add this application as a part of well integrity procedures and recommendations for such like cases.

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