Search engine for discovering works of Art, research articles, and books related to Art and Culture
ShareThis
Javascript must be enabled to continue!

Investigation of the Impact of Realistic Inlet Distortions on a 1.5-Stage Transonic Compressor

View through CrossRef
Abstract In this study the aerodynamic impacts of inlet distortions caused by a gas turbine inlet manifold are analyzed experimentally. The investigation is performed at the new transonic compressor test rig at Technical University of Darmstadt, that features high modularity and extensive instrumentation. The existing axial air inlet system of the test rig is replaced by a scaled inlet manifold. Analog to the design of a real gas turbine intake, bearing support struts are integrated in the experimental setup to investigate their interaction with the inlet distortions. For the detailed analysis of compressor performance, the measurement systems were extended to resolve the flow over the whole circumference at three different axial positions. At the stage inlet a traversable rake with radially distributed five hole probes allows the quantification of the inflow conditions. To determine global compressor characteristics and analyze the propagation of inlet distortions through the compressor, a fully traversable instrumentation at the stage exit is installed. Additionally, a 360°-traversable rotor casing ring, instrumented with unsteady measurement systems, enables the analysis of the effects of non-uniform inflow conditions on the unsteady flow field of the rotor.
Title: Investigation of the Impact of Realistic Inlet Distortions on a 1.5-Stage Transonic Compressor
Description:
Abstract In this study the aerodynamic impacts of inlet distortions caused by a gas turbine inlet manifold are analyzed experimentally.
The investigation is performed at the new transonic compressor test rig at Technical University of Darmstadt, that features high modularity and extensive instrumentation.
The existing axial air inlet system of the test rig is replaced by a scaled inlet manifold.
Analog to the design of a real gas turbine intake, bearing support struts are integrated in the experimental setup to investigate their interaction with the inlet distortions.
For the detailed analysis of compressor performance, the measurement systems were extended to resolve the flow over the whole circumference at three different axial positions.
At the stage inlet a traversable rake with radially distributed five hole probes allows the quantification of the inflow conditions.
To determine global compressor characteristics and analyze the propagation of inlet distortions through the compressor, a fully traversable instrumentation at the stage exit is installed.
Additionally, a 360°-traversable rotor casing ring, instrumented with unsteady measurement systems, enables the analysis of the effects of non-uniform inflow conditions on the unsteady flow field of the rotor.

Related Results

Predicting streetscape green infrastructure performance amidst uncertain inflow
Predicting streetscape green infrastructure performance amidst uncertain inflow
Sustainable cities feature infrastructure that is adaptive to a wide range of spatially and temporally variable conditions. Water infrastructure needs to be responsive to both the ...
The Effects of Wet Compression on Gas Turbine Engine Operating Performance
The Effects of Wet Compression on Gas Turbine Engine Operating Performance
Water, in the liquid or vapor phase, injected at various locations into the gas turbine cycle has frequently been employed to improve engine performance. One such way to improve en...
Achieving the Three Dimensions of Mixed Refrigerant Compressor Efficiency
Achieving the Three Dimensions of Mixed Refrigerant Compressor Efficiency
Abstract Investors in small-scale LNG (SSLNG) face the grave challenge of achieving cost efficiency, operational efficiency, and energy efficiency in the equipment t...
Root Cause Analysis of the Catastrophic Failure of a Propylene Recycle Compressor
Root Cause Analysis of the Catastrophic Failure of a Propylene Recycle Compressor
Abstract A 2-section, 6-stage propylene recycle compressor experienced a catastrophic failure that resulted in extensive damage to its internals. The compressor was ...
Unusual Presentation of Alice in Wonderland Syndrome: A Case Report and Literature Review
Unusual Presentation of Alice in Wonderland Syndrome: A Case Report and Literature Review
Abstract Introduction Alice in Wonderland Syndrome (AIWS) is an uncommon and frequently overlooked neuropsychiatric condition, marked by brief episodes of altered visual and somato...
Centrifugal Compressor Design Considerations
Centrifugal Compressor Design Considerations
Initial design considerations of centrifugal compressor are commonly performed with experience base, although computer technology and numerical methods had made significantly progr...
Multicriteria Optimization of Axial Low Pressure Compressor of Gas Turbine Power Plant
Multicriteria Optimization of Axial Low Pressure Compressor of Gas Turbine Power Plant
The paper shows a method of the gas-dynamic refining of three-stage axial compressor based on the joint usage of mathematical optimization software IOSO and CFD complex NUMECA. The...
Approach to Model Thermistor Based AC Compressor Cut-OFF/Cut-IN Phenomenon in 1D Simulation of Mobile Air Conditioning
Approach to Model Thermistor Based AC Compressor Cut-OFF/Cut-IN Phenomenon in 1D Simulation of Mobile Air Conditioning
<div class="section abstract"><div class="htmlview paragraph">This paper documents the approach followed to simulate the physical phenomenon of thermistor based AC comp...

Back to Top